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  • Writer's picturealexandergardner7

Number 9

This week in class we would on AT commands this is what we will use to turn on the motor with Bluetooth. We successfully turn on a light and made it plus with is simulating the other direction the motor will need to turn in order to turn off and on the lights. However, we did run into many problems with testing the motor in this setup. First, there was a lot of wiring and complex circuitry that was used. This might be faulty due to not having been used in some time. I also could not get the motor to turn this might have to do with the code not accounting for the type of motor. In addtion the battary seemed to be dieing tords the end of the expiements and I did not get a high votalge reading when running the program. I looked over the code and discovered that it was trying to use a dital pin to cotbined with converters to suply the power I sight this a casue for not getting a high reading of the voltage monitor. I think we need to do some more test and detrumin what the next actions for lazy tec. Are going to be the main question of is ardino the right fit is still on the board.

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